This quarter was all about air leakage and energy
efficiency. In order to have an energy efficient house you have to cut off the
air leakage. This keeps the conditioned air in the house that you have paid
so dearly to heat. After the air leakage is cut off then ventilation air is the concern. Living beings, like people, need fresh air to
breath in order to be happy, healthy, and productive. The following is the
process of events leading up to the present state of efficiency for the little
house.
We passed our frame inspection and started to install insulation and sheetrock. Everything on this house has been a bit of a trial and the insulation was no exception. As part of the science of the building we were testing for air leakage at each stage of construction. We first installed the insulation and sheetrock in the ceiling portion and then ran a blower door test, the result was 15 air changes per hour at a negative 50 Pascal air pressure. I was hoping for better, it seemed as though the exterior walls were not as much of an air barrier as I had expected.
Next was to insulate and sheetrock the walls. We used
dense-pack blown-in insulation in the walls that was held in place with netting
until the sheetrock could be installed. This insulation was chosen because the
wall cavities could be filled fully without the voids and compressions that can
be the result when using fiberglass batt insulation. The insulation and
sheetrock went up and another blower door test was conducted. The result this
time was 8 air changes per hour at a negative 50 Pascal air pressure. This
number is better, but still not what we are looking for in an energy efficient
home.
What can be done now you ask? Well we started to tape and mud
the sheetrock. All ceilings, walls, inside corners, outside corners,
transitional areas, and intersecting walls were tapped and coated. At this
point we thought we for sure were going to have built the equivalent of a
thousand square foot thermos on a foundation. The blower door test at this
stage showed 5 air changes per hour at a negative 50 Pascal air pressure. We
are still not at the 1 air change goal that we all thought we were going to be
able to achieve.
So now this is getting frustrating. One thing we noticed
when conducting the leakage testing was the amount of air leaking through the
penetrations in the envelope. Every hole in the envelope was contributing to
our very significant leakage number. I went to the hardware store, bought
caulking, cover plates, insulation pads for under the cover plates, and some
blue tape to cover holes that couldn’t be managed with cover plates.
We covered most everything we could find and the result was to bring the number down to 3.5 air changes per hour at a negative 50 Pascal air pressure. OK, so now were starting to approach an acceptable number. What this shows us is that the devil is in the details, and not just at one spot, but through the entire construction process. We still have some air leakage in the attic areas to seal up and I am confident that once that is done that we will be very close to our goal of 1 air change per hour.
Another thing we were very pleased to discover was that our
heating system is totally within the thermal boundary, which is as planned. The
significance of this feature is that if by chance there should be any leakage
from the heating system, it doesn’t leave the conditioned air space. Hence,
there is no leakage of heated air to outside. This house holds all the air it
heats.
Once again I would like to thank all the students for their
continued support and enthusiasm towards the project. Without their hard work,
critical thinking, and creative ideas this project would not be able to proceed
and be successful. I will leave you with a few more pictures of progress and
fellowship.
Good by and good building,
Dan Smith
No comments:
Post a Comment